An accident happened on loading the cargo in chemical tanker.The crude had to load CST (crude sulphate turpentine),2000 tonnes. The MARPOL annex II gives a category X to the CST.
The crew members were explained onboard before loading but not perfectly or exactly with this type of cargo,they strictly fallowed all procedures and check list, including P&A and SMS of the tanker.
The chief officer gave prior instruction and arrival but the MSDS were missing and the cargo hazards were not explained properly.
The crew received only generic MSDS but the
toxicity of hydrogen sulphide (H2S), organo-sulphides and
mercaptans were not mentioned.
Due to that,only a respirator filter was used by the surveyor
Finally, the seaman and the chief officer were rescued by
The root cause of the accident were found:
3.The strong odor was ignored and breathing apparatus
5.Lack of identification of potential danger, for instance - the
6.The initial rescue attempt was an act of impulse, the chief
The crew members were explained onboard before loading but not perfectly or exactly with this type of cargo,they strictly fallowed all procedures and check list, including P&A and SMS of the tanker.
The chief officer gave prior instruction and arrival but the MSDS were missing and the cargo hazards were not explained properly.
The crew received only generic MSDS but the
toxicity of hydrogen sulphide (H2S), organo-sulphides and
mercaptans were not mentioned.
Due to that,only a respirator filter was used by the surveyor
. This was not effective against the vapours from the H2S.
The Butterworth hatch of the tank was opened by a seaman
who did not even wear a respirator.
The situation was seen by another crew member. He
The situation was seen by another crew member. He
informed the chief officer and then the Master. He sound
the general alarm on the vessel bridge. At that time, the
chief officer tried to save the seaman but he was not
wearing any apparatus, neither was prepared for the
atmosphere. When he approached, he became
unconscious. An attempt to rescue the seaman and the chief
officer was done by another crew member. He held his
breath but still the vapours affected him badly.
Finally, the seaman and the chief officer were rescued by
other crew members who were wearing breathing
apparatus. At the hospital, where they were taken, they were
recovered completely.
The root cause of the accident were found:
1.Insufficient MSDSs version;
2.Inappropriate briefing prior arrival;
3.The strong odor was ignored and breathing apparatus
were not in use;
4.The fixed washing system was defective;
5.Lack of identification of potential danger, for instance - the
place of the Butterworth hatch;
6.The initial rescue attempt was an act of impulse, the chief
officer did not use breathing apparatus, neither the
atmosphere was checked
.
7.The Master did not follow terminal emergency procedures.
7.The Master did not follow terminal emergency procedures.
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